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June 2009 SPE Projects, Facilities & Construction 19 The Cliff Head Field Development—Flow Assurance and Production Chemistry Challenges in a Marginal Field Context Simon Daniel, ROC Oil Company Limited, and Jon Roberts, Advantage Energy Limited Copyright © 2009 Society of Petroleum Engineers This paper (SPE 115612) was accepted for presentation at the 2008 SPE Annual Technical Conference and Exhibition, Denver, 21–24 September, and revised for publication. Original manuscript received for review 7 July 2008. Revised manuscript received for review 30 December 2008. Paper peer approved 13 January 2009. Summary The Cliff Head Field, offshore Western Australia, faced signifi- cant development challenges because of its location and reservoir fluid properties. The influence of these challenges is apparent in the development solution adopted from sandface to market. The modest reserve size required the application of a number of firsts, including coiled tubing (CT), deployed electric submersible pumps (ESPs) combined with intelligent completion technology, a novel water “spike” approach to waxy crude transportation, a distrib- uted chemical injection system, a remote-controlled, normally unmanned production platform, produced water re-injection, and “hydrofrac” water-injection capacity. This paper describes the flow assurance and production chem- istry challenges facing the development, the resulting development solution, and the production history to date. Introduction The Cliff Head field is located in Commonwealth hydrocarbon exploration permit WA-286-P in the offshore Northern Perth Basin, Western Australia. Cliff Head is the first offshore development within the region. The facilities consist of the following compo- nents (Fig. 1): • A minimum facilities, unmanned wellhead platform, Cliff Head Alpha (CHA) approximately 7 miles offshore, to accom- modate the dry well heads and support equipment. • Six production wells with coiled tubing deployed ESPs and two water injection wells on CHA. • Arrowsmith Stabilization Plant (ASP) located approximately two miles inland. • A nine-mile insulated sub-sea production pipeline, crossing beneath the shoreline and the dune system by means of an hori- zontal directionally drilled (HDD) hole. • A nine-mile insulated subsea water injection pipeline from ASP to CHA, also using an HDD shore crossing. • Onshore source water well to supply make-up water for injection. • A subsea umbilical power, control and chemical supply cable running from ASP to CHA. The field was discovered in December 2001 when Brent crude prices were at USD $20 per barrel. The field contains 15.7 million barrels of estimated ultimate oil recovery. The offshore area is host to a variety of marine flora and fauna, including important seagrass meadows and cetaceans. It is also a major rock lobster fishing ground. For these reasons, the offshore facilities have been designed to ensure that no waste will be dis- charged into the marine environment. The onshore plant area is located in a Class C nature reserve. The low energy reservoir is normally pressured with a low solution gas to oil ratio, (GOR, see crude properties, Table 1) and therefore requires water injection for pressure support and artificial lift to achieve economic production rates. Studies indicated that the most appropriate method of artificial lift was ESPs. Considerations such as the remote location, unavailability of drilling rigs, and minimalist production platform, however, meant that the ESP deployment system had to allow for rapid, low-cost, and rigless work-over interventions. These requirements led to the selection of CT-deployed ESPs. Flow Assurance Challenges Initial Well Data. The drilling of the fi eld discovery well Cliff Head 1 in late 2001 yielded formation tester samples providing early indications that the fl uid properties were likely to be prob- lematic for any development. The Cliff Head 3 well test, carried out in January 2003, established that artifi cial lift would be required and confi rmed that the crude was waxy in nature (see Table 1), and contained signifi cant levels of nitrogen, sulphur, and oxygen- bearing (NSO) compounds. The initial fl ow assurance study on Cliff Head stock-tank crude following the fi rst samples reported a wax content of 27%, a pour point of 34ºC, and a wax appear- ance temperature (WAT) of >90ºC. The cooldown viscosity data compared unfavorably with those of the waxiest crudes in the Asia Pacifi c region. Furthermore, testing with pour point depressants (PPDs), known to effectively treat similar crudes, indicated that dose rates of near 3,000 ppm would be required to achieve suit- able rheological properties. It was clear from these early results that pipeline fl ow assurance would be a critical component of the development success. Following additional appraisal wells, a significant sample inven- tory, including low draw-down PVT and atmospheric samples, were recovered from the appraisal wells for ongoing fluid studies. Water Disposal Requirement. Because of the highly undersatu- rated nature of the Cliff Head reservoir, the low GOR, and uncertain aquifer influx, reservoir pressure was likely to fall rapidly upon commencement of production. Therefore, pressure maintenance was considered a prerequisite from day one. Further complications included the high pour point of the waxy crude and the associated thermal issues. The opportunity to avoid discharge of produced water to the sea was afforded by the potential utilization of closed-loop-produced water for water injection supplemented by initial make-up water from an onshore water well. The Phase 1 feasibility study prior to declaration of commerciality defined a water-injection concept and provided refined costs. A second phase of work was then conducted to provide data for the FEED and detail design. The Phase 1 water injection study determined that produced water re-injection (PWRI) was feasible. Water injection up-time was considered critical because of limited water storage onshore, low field GOR, and an assumed negligible aquifer support, re- sulting in rapidly falling reservoir pressure. Therefore, complete and reliable voidage replacement would be required from first oil production. Following literature reviews (for example Cassinat 2002) and because of the high potential for near-wellbore wax deposition and emulsion blocks, it was further determined, following more detailed laboratory studies (discussed next), that heating of in- jection water to a minimum of 55°C at the injection wellheads would be required, at least during initial production. The Phase 2 study showed that fracture injection (hydro-fraccing) to maintain injectivity in spite of fluctuations in injection water quality offered project capital cost savings of up to USD $4 million by removing 20 June 2009 SPE Projects, Facilities & Construction the requirement for high specification filters. Furthermore, deleting operator intensive filtration equipment resulted in significant op- erating-cost reduction. A possible drawback to fracture injection is conformance: the potential for vertical and horizontal fracture growth leading to bypassed oil and nonoptimal waterflood man- agement. However, with detailed modeling of the formation pore throat-size distribution and detailed reservoir geomechanics stud- ies, it was possible to specify the allowable operating limits for injection water solids content and confirm with a high degree of certainty where fractures would propagate. Injection Water Source. An onshore aquifer at a depth of 1000 m capable of providing water at approximately 65°C was selected as the most suitable initial source water. Following a source water well test, it was possible to precisely determine the source water composition and flowing tubing head temperature (FTHT). The FTHT of 65°C was capable of providing some 4 MW of heat-flowinto the production system—a significant low-cost heat source. Flow Assurance Studies Workfl ow and Strategy. The criticality of fl ow assurance at Cliff Head was recognized early, and management of this key project risk was assigned to a single individual. A phased approach was adopted to allow project engineering to progress in parallel with laboratory studies (see Fig. 2). Phase 1 was undertaken pre-FEED and consisted of: • Steady state thermo-hydraulic modeling of the wells and pipeline to provide preliminary assessments of Cliff Head flow assurance issues, particular relating to wax deposition. • Laboratory flow-assurance studies aimed at confirming key flow assurance parameters and providing data to aid in assessing piping and pump size requirements, pipeline restart pressures, and pipeline displacement options. Phase 2 consisted of more focused steady-state and dynamic thermal and hydraulic modeling to remove uncertainty and provide clear design parameters or ranges for the basis of design and opera- tions input. The influence of the key flow-assurance parameters on the facility design are set out in Fig. 3. Phase 1 Flow-Assurance Laboratory Studies. There was a dispari- ty between initial fl ow-assurance results (specifi cally wax appearance Onshore facilities Crude stabilization Export via truck transport HDD Offshore facilities Coastline Development wells Reservoir • Pipeline to shore • Water injection to CHA • Power to CHA • Chemical injection to CHA • Fiber optics Fig. 1—Cliff Head facilities overview. Flow Assurance Studies Project Phases Initial PVT analysis Laboratory FA study numerical analysis Chemical selection Reality check Concept FEED Detailed design Commissioning and operations Fig. 2—Flow assurance studies and relationship to key project phases. TABLE 1—PVT AND FA PROPERTIES Well CH1 CH3 CH3 CH3ch1 CH3ch1 Sample MPSR-192 MPSR-494 11489-QA 11478-QA Depth (m RT) 1280 1276.2 1297.9 DST 1 DST 1 Bo (rb/stb) 1.037 1.047 – 1.053 1.058 GOR (scf/stb) 9 32 – 35 38 Pb (psia) 123 371 – 378 433 Viscosity at 73°C (cp) 6.88 6.25 – 5.53 5.49 Compressibility (10^6/psi) 5.73 5.69 – 5.92 6.67 API gravity 31.4 30.7 33.2 33.0 33.1 Pour point (°C) 36 36 33 33 33 Wax (wt%) 30.2 20.4 20.6 23.7 20.4 Asphaltene (wt%) 0.67 0.59 0.67 0.22 0.25 June 2009 SPE Projects, Facilities & Construction 21 Pour Point. ASTM D5853 is conventionally used to determine the pour point of crude oil. The test is conducted at atmospheric pressure and the method provides maximum and minimum read- ings, depending on the thermal history of the crude. Because of concerns about the usefulness of “dead crude” pour points gener- ated by Labs A and B, an alternative approach was undertaken by Lab C. A “live” crude sample was heated in a pressure cell (held at pressure), to minimize the loss of light ends which may result in an unnecessarily pessimistic result. Once liquid and fully homog- enized, the standard procedure was followed to determine the pour point under atmospheric pressure. Table 3 presents the impact of this procedure modification on the crude’s pour point. A conserva- tive pour point of 32°C was assumed for the pipeline design. Asphaltene Studies. Early examination of Cliff Head crude identified significant levels of black noncrystalline material, rais- ing concerns about asphaltene precipitation. As gas lift was not planned, the major impacts on asphaltene stability would be the pressure drop from initial reservoir conditions. Laboratory testing utilized filter plugging and spectroscopic analysis to assess the asphaltene stability of Cliff Head crude at 73°C and through the expected range of production pressures in 200-psi steps. Slight variations in absorbance and filter pressure drop suggested slight asphaltene instability at 1400–1600 psig (Fig. 4). However, the results generally indicated good asphaltene stability, agreeing with observations made during the well test and comparative data (Jamaluddin et al. 2001), from the high resin to asphaltene ratio (34:1) reported following saturates, aromatics, resin and asphaltene (SARA) benchmarking. Based on the WAT and asphaltene studies, the black noncrystal- line material identified in early testing was assessed as unlikely to present a flow-assurance risk to the development, and further work to characterize it was considered unwarranted. Crude Viscosity. Viscosity measurements at various shear rates were made on fully restored, stabilized, crude under dynamic cool- ing conditions. As with the pour-point work, crude beneficiation was conducted in sealed containers to minimise loss of lightends. Results are plotted in Fig. 5. The key finding was that viscosities remained relatively low until 35°C, indicating that dry crude was unlikely to gel until quite close to the pour point. Pipeline Restart. Environmental conditions for all modeling and laboratory work were worst-case (minimum seabed tempera- ture of 14.5°C). Stabilized dry crude was used for the restart test- ing, again with the aim of representing the worst case due to no beneficial impact of dissolved gas. A model pipeline was utilized as follows: • Test pressure 15 psig confined initially (to prevent light ends losses and counteract shrinkage). Key FEED Design Numbers • Wax content • Asphaltene precipitation envelope • Crude viscosity • Wax deposition rates • Pipeline restart tests • Pour point • Wax appearance temperature “WAT” • SARA and high temperature GC benchmarking • Wet crude/emulsion studies Influence of Parameter → Heating/insulation/pigging → Well/pipeline management/mitigation → ESP specs/pipeline/storage/export → Pipeline/heating/pigging/export → Pipeline/mitigation/pigging/pump sizing → Restart/cool-down timing/pigging/export → Heating/insulation/pigging → Design options/mitigations → ESP specs/chem. inj./pipeline/pigging/vessels /heating/storage Fig. 3—Influence of flow assurance parameters on facilities design. TABLE 2—WAX APPEARANCE TEMPERATURE AT VARYING PRESSURES USING MODIFIED CFPPT Wax Appearance Temperature (°C) Pressure (psig) 55 0 45 150 48.5 1900 10 8 6 4 2 0 2000 1500 1000 500 0 0.3 0.25 0.2 0.15 0.1 In c re a s e A c ro s s F il te r, p s i/ h o u r A b s o rb a n c e Pressure, psig Filter pressure increase Crude absorbance Fig. 4—Asphaltene precipitation run. temperature) and the observed performance of the crude, as refer- enced in the following. Therefore a new fully integrated study, uti- lizing alternative procedures, was commissioned as part of Phase 1. The differing test methods and results are discussed next. Wax Appearance Temperature. As stated previously, in the initial post-discovery work a wax appearance temperature (WAT) of >90°C was determined. The viscometry method was used for this work. This defines the WAT as the temperature at which the viscosity of crude cooled at a controlled rate deviated from a straight line (i.e., shows non Newtonian behavior owing to the presence of solids). The subsequent well test and laboratory work presented no evidence of wax deposition or crystallization at temperatures of 40°C and less. Therefore an alternative method, based on the cold filter plugging point test (CFPPT), was used to further explore the potential for wax deposition in the Cliff Head process. In this method, fully restored crude is flowed through a 0.5-micron filter at a controlled cooling rate, while the differential pressure across the filter is monitored. In this experiment, the WAT is defined as temperature at which irreversible plugging of the filter commences and a deviation from Newtonian behavior occurs. The method presented a significantly lower WAT (see Table 2) more in line with field and laboratory observations. TABLE 3—POUR POINT BYLABORATORY Laboratory Pour Point (°C) Source Sample Lab A 33-36 CH3 dead crude Lab B 34 CH3 dead crude Lab C 26 CH3 live crude 22 June 2009 SPE Projects, Facilities & Construction • Coil dimensions 160-in. length by 0.18-in. internal diameter. • Applied restart wall shear rate of 1 sec-1. Two shutdown conditions were considered aimed at represent- ing the following cases: 1. A sudden shutdown from normal operating conditions— pipeline bulk fluid temperature assumed to be 60°C 2. A slow turn down from operating conditions to just above the pour point (35°C) before shut-down. The sudden shut-in case resulted in a higher restart pressure because of the development of a gel/solid phase with a relatively high yield stress. Static cooling from a higher temperature allowed more effective crosslinking of the wax crystals. Shearing during cooling inhibited crystal growth, resulting in correspondingly lower apparent gel strengths. Upscaling the results indicated that pumping requirements for displacing the offshore nine-mile product pipeline of dead crude should be sized to provide start-up differential pressures of at least 1,230 psig across the pipeline (Table 4). It is important to note that the crude does not become liquid once the restart pressure has been reached. The pressure indicated is the “breakaway yield stress” of the crude plug. Handling of the solids associated with the mobile plug following a cold restart required consideration within the facilities design. Wax Deposition Rate. Predicting deposition rates from labo- ratory testing is somewhat qualitative despite best efforts to mimic expected field conditions. Furthermore, there are numerous laboratory procedures that purport to provide the most accurate approximation. The method used involves pumping suitably con- ditioned crude at a constant shear rate through a calibrated test loop (1/4-in. OD × 12-in. tubing) held at a specified temperature while continuously monitoring pressure differential across the test loop. The estimated wax deposition rate for that temperature is then calculated using the test loop data. The approach allows for detailed measurement of deposition rates at various points in the modeled pipeline based on the thermal gradient. To ensure that shear-related factors (shear stripping) are considered, flow at several shear rates is modeled. Again, the fluid tested is dry, dead oil as the worst case. Deposition rates were consistently very low for this crude. The worst case, when upscaled for the offshore product pipeline, gave a deposition rate of only 1.0 × 10–3 in. per month, adjacent to the location in the pipeline where the temperature fell below the WAT. Low deposition rates reported in this testing agreed with the well-test results, in which no signs of wax deposition were detected in the tubing or flowlines, despite known periods of bulk liquid flow below the WAT. Furthermore, the crude viscosity results reported previously implied a relatively low degree of wax precipi- tation in the crude sample below the WAT and down to 35°C. As noted previously, anecdotal laboratory evidence during handling and observing the crude under various cold surface conditions directionally supports these results. Emulsion Characterization. Shearing with differing ratios of Cliff Head crude and synthetic formation water showed the emul- sions formed readily and remained stable up to approximately 60% water cut following conditioning at high shear rates to simulate ESP production conditions. Viscosities of the emulsions were significantly higher than those of dry crude, and increased with increasing watercuts, particularly at low test shear rates. Bottle testing by several laboratories and with a range of de- mulsifiers failed to identify any product that significantly resolved high shear emulsions within the specified (1-hour) test period. In combination with the emulsion viscosity data, these results indicated that use of ESPs would produce stable, high-viscosity emulsions that would seriously impact pump sizing, hydraulic design, and operating practices. Experience elsewhere had shown that dosing demulsifier to the ESP suction provided excellent dispersion of the chemical and could result in rapid emulsion resolution. Laboratory testing confirmed that this was also effective with Cliff Head crude. Pour Point Depressant (PPD) Assessment. PPDs (or wax crystal modifiers) work by precipitating with waxes in the treated crude, distorting their crystals and inhibiting deposition. To be effective, a PPD should ideally be dosed to the crude before there has been any crystal growth. PPDs themselves generally require significant preconditioning facilities and can provide handling is- sues in an offshore, normally unmanned environment. Initial testing with Cliff Head crude indicated that very high treatment rates (3,000 ppm) would be required to achieve the de- sired rheological properties. More detailed screening of the four main families of PPD chemicals also failed to find an effective product. Poor lab results, handling difficulties with the product, and the requirement to dose above the WAT of the crude ruled out PPD treatment as an effective flow assurance option for Cliff Head. Core Annular Flow Assessment. Core annular flow (CAF) was identified as a potential transportation method for waxy crudes at temperatures below their pour point (Joseph 1997). This form of transport relies on establishing water as the external liquid phase (in contact with the pipeline wall) and carrying the crude as an internal slurry. The stimulus for investigating CAF at Cliff Head was an export option that involved transporting crude from ASP by an onshore pipeline approximately 60 miles to the nearest port for storage and export by marine tankers. The testing method utilized drilling mud aging cells rolled at decreasing temperatures and then held static at 4°C, the anticipated minimum onshore air temperature. A range of dispersants and water-wetting surfactants were tested. Results were promising, with several of the surfactants maintaining water as the external phase with little crude deposition on the cell walls at dose rates of 200 ppm and temperatures near 20°C. Subsequent tests by another laboratory were also encouraging but indicated that higher chemi- cal treatment rates (1,000 ppm) may be required. The marine export option, and hence requirement for the onshore pipeline, was dropped during FEED in favor of road tanker trans- portation, eliminating a major flow-assurance challenge. Therefore, 1000 100 10 1 20 30 40 50 60 70 80 V is c o s it y , c p Temperature, °C 340 sec-1 170 sec-1 132 sec-1 66 sec-1 13.2 sec-1 Fig. 5—Dry crude viscosity at varying shear. TABLE 4—PIPELINE RESTART RESULTS Conditions Restart Pressure (psig) Across 9 Mile Pipeline Restart Pressure (psig) Across 60 Mile Pipeline Sudden shut-in 1230 7380 Slow turn-down 870 5220 June 2009 SPE Projects, Facilities & Construction 23 the CAF option, despite providing promising results, was not pursued further. Phase 2 Flow Assurance Steady-State and Dynamic Modeling. Numerical Simulation and Transportation Considerations. The full life cycle crude rheology results from the Phase 1 fl ow assur- ance laboratory studies were incorporated into a steady-state mod- el, including the envisaged pipeline route and elevation changes. A constant U value of 1 W/m2K was assumed for all cases for the onshore section of the pipeline, which was to be trenched and buried in dry sand. The nine-mile product pipeline from the off- shore platform to the onshore plant was modeled, given a required arrival temperature above the defi ned WAT of 45°C. The following was to be determined: • Insulation requirements (type, thickness, and so on). • Pipeline pressuredrops (c.f., ESP deliverability • Operational considerations of start-up/shut-down. Pipeline Insulation Requirements and Water Spike. The mod- eling strategy for the production pipeline was such that if the arrival temperature could not be met, alternative insulation options, plus a novel hot water spike approach, would be applied. Other pipeline developments have utilized hot steam spikes to add thermal mass to the bulk fluid in an attempt to maintain flow properties (Tang Y. et al. 2003). In this case, an option for consideration was spiking the 55°C hot water available offshore through the insulated a hot water injection pipeline for water injection with the produced fluids. The benefits of this approach are as follows: 1. Thermal mass of bulk fluids would be increased and a com- mensurate reduction in insulation possible. 2. Above the emulsion inversion point (here, circa 60%), bulk liquid viscosity would reduce. 3. Adding water to a dry crude pipeline would reduce the gelled pipeline restart pressures. 4. Providing the ability to add agents to the offshore produced fluid in the aqueous phase as a mitigation option should insulation prove ineffective (e.g., slurrification additives for CAF). Initial simulations demonstrated that at low water cuts, insulation was indeed necessary to prevent the stream falling below 45°C before arrival at the plant. With inlet temperatures of 65–70°C and the most optimistic field water rate, all cases without insulation fell below the pour point before reaching the pipeline halfway point. Even with 35,000 B/D gross liquid, 97% water cut, and an inlet temperature at 100°C, the model showed pipeline fluid temperature reaching the pour point some four miles before the end of the nine-mile pipeline. The next stage of testing was aimed at assessing insulation requirements in early field life with low water cuts, and com- mensurate low thermal mass, but including the option to use the thermal water spike. Table 5 illustrates these results for a fixed inlet temperature of 50°C, a realistic low rate case. These results indicate that for a U value of 3 W/m2K, hot water injection was required to meet an onshore arrival temperature of 45°C. Hot water at 55°C would need to be “spiked” into the line at the offshore platform to provide an additional temperature boost and greater thermal mass. As expected, the greatest demand for hot water was when the field water cut was lowest. To study the impact of reduced insulation on the heated water requirement, a case of U = 11 W/m2K was considered with a 65°C inflow temperature. Results showed that hot water of 60,000 B/D at 55°C would be required for an early field life case of 20,000 BOPD. For only 5,000 BOPD, the heated water requirement was still 55,000 B/D. Therefore, U = 11 W/m2K was not feasible for these cases. Steady-state results indicated that, with the expected minimum seawater temperature, cooling of the offshore pipeline system would be significant. Insulation of U = 3 W/m2K plus a 55°C hot water spike was required to meet the onshore arrival temperature of 45°C for expected field oil and water production rates. It was further expected that pipeline insulation and the use of thermal spike water would help minimize the potential for wax deposition in the pipeline. Production Pipeline Pressure Drop Requirements. To real- istically imitate expected field conditions, including the impact of untreated emulsions, a number of cases were run with varying viscosity profiles. The set arrival pressure at the onshore facilities was 150 psig. Viscosities were selected from the laboratory data, based on the field water-cut, prevailing pipeline temperature, and expected pipeline shear rate. The worst-case inlet pressure of 280 psia was within the capa- bilities of the downhole ESPs (Table 6). However, power require- ments and well productivity would be improved if demulsifiers were injected as deep as possible in the well-bore, but at least upstream (downhole) of the submersible pumps. Further Numerical Modeling Work. To provide robust data for input into the detailed facilities and pipeline design, further numer- ical modeling addressing the transient behavior of the entire well, gathering, and pipeline system was commissioned. This phase of work was concerned specifically with detailed steady state/dy- namic thermal and hydraulic analysis. Output from this work was incorporated into more detailed project risk assessments. Flow Assurance Solutions Description of Facilities. The laboratory testing and modeling programs described previously identifi ed fl ow-assurance-based design, equipment, and treatment criteria essential for the develop- ment of the Cliff Head fi eld. These are listed in the following: TABLE 5—STEADY-STATE MODEL ING RESULTS (50°C INLET, HOT WATER SPIKE) Oil Rate (stb/d) Field Water Cut (%) U (W/m 2 K) Hot Water (bbls/d) 18250* 27 3 0 18250 27 3 7500 10440 64 3 3000 6000 80 3 2000 * case failed to meet specified onshore inlet temperature TABLE 6—STEADY-STATE MODEL ING RESULTS, PRODUCTION PIPELINE PRESSURE DROPS Case Inlet Pressure (psia) Pressure Drop (psi) 190 cp No demulsifier, high water cut 280 116 50 cp No demulsifier, early field life case 260 96 12 cp Demulsifier added, high water cut 213 49 24 June 2009 SPE Projects, Facilities & Construction Wells: 6 producers and 2 water injectors. • Downhole demulsifier injection into the suction of the ESP. • Downhole combined corrosion and scale-inhibitor injection. • Ability to circulate the wells with hot injection water to re- move waxy oil from the production string and deliver or displace treatment chemicals if required; the completion details have been reported elsewhere (Way et al. 2007). • Production tubing to casing annulus vacuum from mud line to platform tree to help prevent cold spots in the production tubing through the water and air gap. • Crude produced above the saturation pressure upstream of the choke to mitigate solids (asphaltenes, etc.) and allow simple surface remediation. • Downhole monitoring and flow-line metering to allow ESP health and performance tracking and monitoring of pump scale and fouling. Platform: (not normally manned). • Insulation and heat tracing of all surface production piping and instrumentation. • Distributed chemical injection system fed through a subsea umbilical. • Offshore injection water quality monitoring (online turbidity meter). • Hot water injection water spike to add thermal mass to fluids in the production pipeline. Pipelines: (1 × production, 1 × injection). • Identical 10-in. injection water and production pipelines on piggable loop. • 0.563-in. wall thickness, (1500# ANSI), sized for hydrofrac and gelled pipeline restarts. • Polyurethane foam insulation and concrete weight coated (0.984 in./1.575 in.). • U Offshore =3.0W/m2K. • U Onshore =1.0W/m2K. Onshore Plant. • Heat tracing of all production piping and instrumentation. • Lagging and heating medium circuit through all vessels and storage tanks. • Onshore source water well to provide heat flow into the system. • Downhole combined corrosion and scale inhibitor injection to source water well. • Capability to reroute gelled pipeline contents to settling tank. Water Injection Facilities. • High-pressure onshore positive displacement pumps for hy- drofrac produced water-reinjection scheme. • Induced gas flotation for oil and solids removal (hydrocy- clones may be problematic with waxy crudes). • Water injection pumps sized to allow displacement of cold, gelled pipeline. Operational Flow-Assurance Summary There have been a number of flow-assurance challenges since the field was commissioned in mid-2006; however, none were related to crude gelation, wax deposition, emulsion stability/viscosity, or pipeline re-start pressures. Facility uptimes have been excellent, with only 5 hours of downtime in 2007. Flow-assuranceparam- eters investigated in laboratory testing and modeling and mitigated against in field planning are addressed in the following: • The crude is waxy with an ASTM 5853 pour point of 32°C. • Production pipeline temperatures are maintained at >55°C, and weekly pig runs have never recovered hard wax deposits, confirming that the WAT is below this temperature. • Pressures in producing wells are maintained above the bubble point of the crude, and there are no indications that asphaltene deposition is occurring downhole or anywhere in the process. • At least 50% of the production pipeline volume is made up of hot water and it is displaced with hot water prior to planned shutdowns, so the pipeline restart calculations have never been challenged • Crude is exported hot (>55°C) and loses very little temperature in the 5–6-hour journey to the refinery. High dry crude viscosities have, therefore, never had an adverse impact on field operations. • Emulsions generated by the ESPs are extremely stable. Centri- fuged at 1,600 rpm and 70°C for 30 minutes, an untreated wellhead sample with >40% water cut will typically drop only 1–2% water. However, effective demulsifier treatment followed by 4 hours in laminar flow in the production pipeline containing >50% hot water produces emulsion-free near dry oil in the production separator. • Because of the effectiveness of the production system, no additional PPD or CAF testing has been undertaken. Facilities heat flows (Fig. 6) were generally within expectation and the pipeline insulation has performed well (Table 7), despite M /T HDD Onshore - buriedSubsea Platform 1 3 4 5 6 7 9 2 8 11 33 44 55 66 77 99 22 88 Steady-State Relative Heat Flow In 1 4000 kW 2 2200 kW 3 2500 kW Out 4 Negligible kW 5 1000 kW 6 4600 kW 7 1000 kW 8 2100 kW Transfer 9 350 kW Fig. 6—Cliff Head facilities steady-state heat flows. June 2009 SPE Projects, Facilities & Construction 25 TABLE 7—OPERATIONAL PIPELINE INSULATION PERFORMANCE Parameter Detailed Design Estimate Field Experience U Overall 2.5 W/m 2 Kcompounds present—possibly Greigite (see above). There were also some iron oxide compounds present, perhaps owing to oxygen attack. A detailed survey of the onshore plant failed to detect signifi- cant levels of oxygen in either produced or injection water. Howev- er, visual inspection during the Year 1 shutdown found significant pitting and oxygen corrosion product on pump discharge lines on the injection water system. Finally, recording gauges mounted on several of the standby pumps showed them regularly going into vacuum, indicating that air ingress was likely through mechanical seals. Continuous oxygen scavenger injection was initiated imme- diately, and high sensitivity corrosion monitoring probes recently installed in the injection water system indicate that negligible metal loss is occurring. Alternative seal options and the mothballing of possible air ingress sources (such as the IGF) are under review. Conclusions Cliff Head field is small oilfield (30°C and high emulsion forming tendencies. The field is located in highly environmentally and economically sensitive, shallow (20 m) ma- rine environment seven miles off a predominantly lee shore. The field was successfully developed because: 1. Flow assurance challenges were recognized early. 2. Appropriate resources were assigned to investigate and develop potential solutions to these challenges. 26 June 2009 SPE Projects, Facilities & Construction 3. The development team was willing to integrate flow-assurance so- lutions into the field development plan and adopt innovative well completion design and pipeline thermal management systems. The development plan has proven robust with respect to waxy crude flow assurance, with cumulative production passing 6 mil- lion barrels in April 2008. Acknowledgments The authors would like to thank the Cliff Head joint venture for its willingness to publish these data and operational history. We would also like to thank David Brankling of Oil Field Chemical Technol- ogy Limited, Chris Payne of Plexal, and Chin The and Jason Jordan of Advanced Well Technology for the significant contribution they and their associates made to the project. References Cassinat, J.C., Payette, M.C., Taylor, D.B., and Cimolai, M.P. 2002. Opti- mizing Water Flood Performance by Utilizing Hot Water Injection in a High Paraffin Content Reservoir. Paper SPE 75141 presented at the SPE/DOE Improved Oil Recovery Symposium, Tulsa, 13–17 April. DOI: 10.2118/75141-MS. Jamaluddin, A., Nighswander, J., and Joshi, N. 2001. A Systematic Approach in Deepwater Flow Assurance Fluid Characterization. Paper SPE 71546 presented at the SPE Annual Technical Conference and Exhibition, New Orleans, 30 September–3 October. DOI: 10.2118/71546-MS. Joseph D.D., Bai R., Chen, K.P., and Renardy, Y.Y. 1997. Core-Annular Flows. Annu. Rev. Fluid Mech. 29: 65–90. DOI: 10.1146/annurev.fluid.29.1.65. Tang, Y., Shuler, P.J., Cheug, S.K., Goodgame, J.A., Hsu, J.J., and Padilla, A.V. 2003. Improved Transportation of Waxy Crude Oils and Emul- sions in Bekasap Area Indonesia. Paper SPE 80243 presented at the International Symposium on Oilfield Chemistry, Houston, 5–7 Febru- ary. DOI: 10.2118/80243-MS. Way, C., Daniel, S., Bird, E., Jordan, J., Guatelli, V.J., and Bettridge, J.M. 2007. Cliff Head Intelligent Completion With Coiled Tubing Deployed ESPs—Increased Production, Reduced Life-Cycle Cost. Paper SPE 108381 presented at the Asia Pacific Oil and Gas Con- ference and Exhibition, Jakarta, 30 October–1 November. DOI: 10.2118/108381-MS. Simon Daniel has over 17 years of geographically diverse oil and gas experience with operating oil companies, field service companies, and consultants in west Africa, the Middle East, the North Sea, and Australasia. His field development exposure includes mature field regeneration in the North Sea, three FPSO developments in west Africa, and both onshore and offshore marginal fields in western Australia. He is currently manger of production and development for ROC Oil Company. Daniel holds a BEng degree in mechanical engineering, an MSc degree in exploration geophysics, and an MSc degree in petroleum engineering, all from Imperial College in London. Jon Roberts started working as a mud engineer in 1974 and became increasing involved in production chemicals over the following decade. He set up a consultancy in the early 1990s and has worked on flow assurance and integrity issues on numerous developments and facilities in the Asia Pacific region since.